Evolution IX – a new turbo and a new problem

October 25, 2009

Many of you out there have been waiting impatiently for the installation of the Tomei turbocharger in the Evo IX.  Believe it or not, I have too.

A couple of weekends ago I started on the installation with great hopes of sharing the experience with all of you.  While I did accomplish the installation I have run into a significant problem that prevents me from concluding this chapter.  After installing the new turbo and radiator the first test drive ended with a check engine light and a P0500 code. 

In order to save you some time in looking up the P0500 code, it refers to the vehicle speed sensor that is built into the transmission.  Fortunately there is nothing wrong with the speed sensor, but there continues to be a voltage problem that prevents the ECU from reading the sensor.  I will continue to track down the source.

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In the mean time I will provide you with the adventure of installing the Tomei ARMS turbo.

First step was to make certain that I had everything I needed and then get the car up in the air.  Luckily Jim’s Garage has a lift that makes getting the car up to a nice working height a snap.  I had spent the previous days making stops at auto supply stores to get fresh anti-freeze and distilled water as well as all the appropriate fasteners for the installation.

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With the car up in the air it was time to remove the under-tray that covers the bottom of engine bay.  This consists of unfastening twenty to thirty “scrivets” and a few screws.  If you own one of these cars it is a good idea to have plenty of spares on hand, too.

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With the under-tray out of the way I drained the coolant into a catch pan.  That gave me a chance to undo several items from the top of the engine compartment.  The air intake was removed along with the heat shields over the stock turbo.  Then I loosened the radiator hoses and worked on removing the O2 sensor.

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From under the car I removed the bolts and springs that hold the down-pipe to the turbo as well as the factory bracket that holds the turbo to the engine block.  It was also a good time to get another catch pan and unbolt the oil return from the turbo.  This goes from the turbo to the oil pan and since Tomei provides new gaskets, I removed it completely and cleaned up the piece.

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With the radiator drained it was time to pull the old radiator.  A ten thousand mile radiator is not necessarily and old part, but this one had a bunch of wrench rash on it.  There was a new Mishimoto unit ready and waiting for installation.  I did find that I had to purchase some rubber bottom mounts as the ones on the old radiator were either worn or incorrect.  I found it easier to remove the radiator fan and motor than to try and pull it as one assembly.

There were two nuts and two bolts holding the turbo to the exhaust manifold and I removed them.  With the radiator out there was plenty of room to remove the turbo assembly. 

Then began the job of installing the new O2 sensor housing on the new turbo with all the new gaskets that Tomei supplied.  There were also new tubing for oil and coolant to the turbo.  These came with new banjo bolts and crush washers.  It was easiest to install them before the turbo was bolted on.  Minor tweaks to the tubing were made by sticking a Philips screw driver in the tubing and gently reforming them. 

With everything bolted to the turbo and fasteners torqued to the proper specifications it was time to bolt on the new unit.

The folks at Tomei really make a nice unit and it bolted up just as the factory turbo had.  I used fresh fasteners and torqued them to specs, too.  Then I installed the O2 sensor and plugged it into the connector on the valve cover.   Next was the down-pipe bolts and springs.  I ran the threads through a die and coated them with anti-seize before bolting the pipe up.

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The radiator was next.  I had to wait a few days for the parts from Mitsubishi to arrive, but they did and the radiator and fan slipped in place.  New Samco hoses were used and a 50/50 mix of antifreeze and distilled water was mixed and installed using an AirLift tool.  The AirLift uses compressed air to create a vacuum in the cooling system.  It lets you know right away if you have a leak and when all is right the tool uses the vacuum to suck in all the new fluid.  It is really a fool proof method of ensuring there is no trapped air in the cooling system.

With that task completed it was on to the intake system.  I had to be careful to ensure that tubing and clamps would not interfere with the electric fan since things had gotten just a bit tighter in that area with the new radiator.

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When everything was buttoned up I did a final check of connectors, clamps and bolts before I turned on the engine. 

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I let the engine warm up while I went over a few more things and put away wrenches.  I was so looking forward to the first drive.  It lasted about 100 yards before the CEL and then the engine started running far too rich.  So back into the garage and continuing problem determination.


Donna Mae Mims

October 14, 2009

“Think Pink” was her standard  and most of her race cars were.  Donna Mae Mims died at the age of 83. She was quite a lady.

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Automotive Challenges and Solutions

September 17, 2009

In December of last year Automotive News published that Toyota’s Japan market Crown luxury sedan went from 60 MCUs to just four.  This news quickly spread across the automotive industry as car manufacturers sought to reduce the complexity and weight of the existing networks of processors and wiring that permeate modern motor vehicles.

Your typical car contains 25-35 microcontrollers and luxury cars have 70 or more.  Connecting all the sensors to those controllers as well as interconnecting the processors to ECUs is the CAN (Controller Area Network) which currently has a data rate of 1Mb/sec.  Another proposed standard is FlexRay which is designed to move data at a rate of 10 Mb/sec.  Motorola has been experimenting with a network design they call Switch Fabric that should move data at a rate approaching 2 Gb/sec.

Automotive designers and manufacturers are struggling to reduce the weight of cars as the demand for more processors and the cabling necessary network them and their sensors increases.  Manufacturers admit to their mid-range cars containing 45 to 65 pounds of wiring, but the figure is likely much higher and especially for luxury cars.  Reducing or eliminating the weight of wiring can drastically improve fuel economy.  Some cars are using Blue Tooth to communicate from switches to controllers in order to eliminate wiring.

The term domain-based computing is being used in automotive design and as a result is more multi-core processors and moving current systems to 32-bit architecture.

Today 32-bit microcontrollers are used in engine, transmission, navigation, ABS, entertainment, GPS, and stability control.  Sixteen bit MCUs are used for SRS (air bags), body control, instrument panel clusters, even HUD.  8-bit controllers are used on power mirrors, door locks, HVAC, radios, CD players, lighting, anti-theft, seat controls, power windows, etc.

With hybrid cars coming into the car population in ever increasing numbers as well as a smattering of electric cars, micro processing needs are ever increasing.  Regenerative braking, power management, and multiple battery systems require more processing, networking, and programming.  Oh yeah, and more wiring.  That’s right, I said multiple battery systems.  As more systems are employed the electrical demands are soon outstripping the capacity of a single 12-14 volt electrical system.

New regulations concerning collision avoidance systems, passenger SRS systems, multimedia, etc., will require more of the above.  If our homes were this integrated we would be paying five times as much for the privilege of having a roof over our heads.

On the bright side, Philips Electronics has released the LUXEON Altilon power LED headlamp. 

While we have seen LED technology employed in automotive and truck taillights as well as in traffic signal controlled intersections, it is now advanced to the point that it can be used to light the road ahead. 

Audi now uses this LED lighting in the R8 headlamps for both high and low beam functions as a $5000 option.  These provide more than 850 lumens with a color temperature of 5600K that conforms to both ECE and SAE specs.

You can expect pricing of this technology to drop dramatically as it becomes the new lighting standard that will not only enable far more flexibility in vehicle body design, but also dramatically reduces power consumption for lighting.  LED life is also far longer than conventional bulb technology and produces far less heat energy.

Soon your eyes will have to adjust from dealing with the HID blue headlight beams to the LUXEON LED wave length.  You can expect conversion kits for existing HID headlamps, too.


Eye Candy from Germany

September 16, 2009

A good friend of mine returned from some vacation time in Germany and sent me these fantastic photos of just a few of the cars he got to see up close:


Evolution 9 – the turbo has arrived

September 13, 2009

While I was away on a three week road trip to New England a package arrived and it contains the Tomei ARMS turbo upgrade I have been impatiently waiting for since I ordered it in mid-May.

The folks at Kami Speed have been very understanding of my frustration and kept me informed as to the status whether it was good news or not.  Apparently the Tomei turbo has been more of a success than expected and production has barely been able to keep up with demand. 

Fortunately Tomei insists on maintaining quality no matter what and that translates into my long wait.

Here are some photos of the turbo along with a really nice O2 sensor housing that will be added to the Tomei kit.  This housing is from a company called Exotic Speed that produces this beauty out of stainless steel.  On my Evo 8 I had used a nicely welded up stainless steel version from eBay that I really liked and was looking for another one for this car when I came across the Canadian company that was selling these.

Next I have to set aside a weekend to install the new turbo, the Mishimoto radiator, and what ever else has stacked up on the bench.

There will be more on that weekend and photos of course.


The Police Car Perfected

August 29, 2009

I have been busy enjoying an end-of-summer road trip to New England for the past week.  Now I am spending some time on Cape Cod renewing acquaintances with relatives and old friends.

As I drive around on highways and byways I am always on the lookout for a police vehicle as traffic law enforcement continues to be an excellent source of revenue without the procedural bother of hiking taxes.

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Now a new automotive manufacturer has arrived on the American scene to produce police cars exclusively.  Carbon Motors has designed a prototype that is diesel powered and fully integrated with lights and computer equipment.

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This is a police car that perhaps Mad Max would envy as it produces 300 hp from a turbo diesel and 400 lb/ft of torque.  Being diesel its fuel consumption is modest and it sport clam shell doors for ease of loading prisoners in the back seats.  The rear compartment is sealed off completely from the officer’s cabin in the front so that the prisoner can pee and barf to their hearts content without making a mess of the front.  Something that is a real problem with today’s police cars. 

The rear seat is a one-piece molded affair that has indentions for handcuffed hands.  It has plugs in the floor so it can easily be hosed out and returned to service quickly.

The front cabin is decked out in the latest electronics and instead of switches to locate and reach for many are voice activated.  Gun racks are built in to the area between the seats and the seats are formed so that the officers can sit comfortably with their sidearm belted on.

On the outside all the usual flashing and blinking lights are built in to the body work.  Normally these things are supplied by aftermarket companies and bolted on and wired in to the police cars.  With their being integrated into the body work the car’s aerodynamics are much improved, too. 

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The push bar is integrated into the front bumper as well.  This also translates to better aerodynamics and eliminates the need to drill mounting holes and bolting up to the frame of the vehicle.

The life of this vehicle is projected to be 250,000 miles which should make it cost effective.

The manufacturer is claiming that it has thousands of pre-orders and will start fulfilling them in 2012 from its Indiana manufacturing facility.

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This is quite a departure from the traditional source of police cruisers where a standard sedan is offered with heavy duty equipment such as a larger capacity alternator and bigger brakes that is then decked out in aftermarket lights, electronics, push bars, and other items.  While not specified by Carbon Motors, the price is expected to be similar to a fully accessorized police car.

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So when can the Blues Brothers get their own pre-owned Carbon Motors E7?  Never.  Carbon Motors is going to sell to law enforcement exclusively and with the stipulation that these cars can never be sold to the public.  Sorry Jake.


A New Project Miata – part two

August 15, 2009

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Today we put more time into perfecting the Miata.  The bump stops for the rear shocks showed up so that was the first order of business.

Removing the shock/spring assemblies means removing all the trim pieces from the trunk as well as unbolting the gold colored steel plate that covers the fuel lines in order to gain access to the top shock bolts.  Once those were loose and removed we put the car up in the air (on the lift) and removed the wheels. 

The anti-roll bar was disconnected, so was the lower shock mounting bolt, and then the upper control arm bolt so it could all be pulled down and the assembly could be removed.

With the Swift springs it was possible to undo the top nut and take the top parts off the shock so the new bump stops could be slid on to the shock rod.  The new bump stops also had to be cut down by one hump as per the Swift instructions.

Both shock/spring assemblies were re-united with bump stops and returned to their place in the rear suspension.  The bolts were tightened and the nuts for the anti-sway bar links were also fastened down.

While the wheels were off we put them on the Hunter balance machine again.  There was a minimal vibration from the rear that I wanted to track down.  Sure enough they were not only out of balance, they were out of round.  Fortunately, the Hunter technology tells how to re-mount the tire in order to make the assembly as round as possible.  Then they were dynamically balanced. 

Then the front wheels were also removed because the stock flexible brake lines were going to be replaced with braided stainless steel lines.  This results in a firmer feel at the brake pedal as the new lines don’t expand and flex with pressure to the degree that the stock ones did.

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Since a lot of brake fluid was going to leak out during the lines swap it also was a good time to flush the brake fluid and we chose Ate Super Blue fluid.

We use a vacuum method of bleeding that allows us to keep the old fluid from contaminating the new fluid as well as eliminate air bubbles that would create a spongy feel.

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After the new lines were on and new fluid was flushed through (including the hydraulic clutch) we changed out the fuel filter for a new one. 

The owner and I had experienced at times when the engine would cut out and lose power, especially when the fuel tank was getting low.  Since this car was ten years old and had been sitting idle a lot we figured that the gasoline was not only old, but had been subject to condensation as temperatures varied by season.  This would be caught by the fuel filter, but it would also clog and impede fuel flow to the point pressure would cut out.

Changing out the fuel filter is a bit tricky.  We are dealing with gasoline, after all.  We had to release pressure in the system by first taking the gas cap off and then pulling the electrical connection to the pump relay.  Then cranked and ran the engine until it would not run.  That released any residual pressure, but there was still plenty of fuel in the lines.

We made sure that we had something to safely catch the dripping gasoline as we disconnected the lines to the filter.  Then we moved the white nylon plastic clips to the new filter so the lines could be snapped on.  Then we secured the filter’s clamp and covered it with the black plastic protector.

The wheels were bolted back on and the lug nuts were tightened to the proper torque before we took the car out for a test drive.  Before we got more than a few feet we discovered that one of the new rear brake lines was touching the wheel so we put it back on the rack and were able to reorient the fitting with no trouble.

The test drive was fine with no other problems discovered, so it was on to the alignment rack.

We knew that the setting would change when we installed the Swift springs on the new Koni shocks since the ride height was lowered.  We also were looking for an opportunity to add in additional caster to the front.

The rears started out with over two degrees of negative camber.  That was much more than the car needed and would keep it from having the kind of rotation you would expect out of a shorter wheelbase car.  We also wanted the total toe to be as close to 0.30 degrees as we could so we chose to set rear camber at negative 1.8 degrees.  Moving to the front we found we could get almost six degrees of positive caster.  That was really great to see.  With a little less caster I could have gotten more negative camber, but in this application the caster was more of a priority so I left the front at negative 1.2 degrees and kept the “almost” six degrees of caster.  Toe would be set at 0.30 degrees total like the rear.

Why so much emphasis on the caster number?  Caster does a lot of different things for your handling and when it is set up to complement a suspension it can be a wonderful friend.  If it is not, it can be unfriendly.

Caster will allow your steering to center itself easily after you are done with a turn.  It will also add camber to the outside tire as you execute a turn.  When you brake it can lessen nose dive and therefore weight transfer substantially.  If you cannot achieve adequate caster you will start to lose all that helpful stuff.

With the alignment complete another test drive was in order.

It was a blast.  Now the car really felt like the happy little convertible it should be.  Corners could be pushed and the rear end controlled much more with the throttle.  The steering felt even more connected with the tires.  This car had really come together.

On Monday a set of FM anti-sway (anti-roll) bars were delivered and installed.  These bars were just a bit stouter than the stock bars an offered adjustability as well.  We were now anxious to and see how much flatter it would handle. 

Now the car really woke up and handled like a pocket rocket.  It made the most of the Bridgestone Potenza RE11 tires and the suspension really followed the contours of the road.  This is one fun Miata!

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A New Project Miata – part one

August 10, 2009

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If you look back on some of the past entries you will find a few on work that was done on a 1996 Mazda Miata.  That car came to us with some modifications that, while performance oriented, left it with a ride that was harsh and unfulfilling.  After performing some maintenance we worked with the owner to choose a better suspension package as well as some much needed frame stiffening.  We also added a roll bar for additional safety.  The owner was very satisfied with the results.

This year the owner decided to transfer ownership of that Miata to one of his sons.  The logistics of delivery meant that he drove it about half way to Texas.  On the way he found the car so enjoyable that he let us know that he was going to find another Miata to replace it and wanted us to think about how it could be modified to duplicate the fun of the 1996 one.

In a week or two he located a 1999 Tenth Anniversary Edition that had barely seven thousand miles on it.  So we set to work evaluating the new purchase and getting a list of parts and pieces that would make it the kind of Miata he yearned for.

The car came with original tires that were aged to say the least.  While the car had been stored with great care the tires really were shot.  We set about to shod it with rubber that would give us the best possible starting point, a set of Bridgestone Potenza RE11 tires.  Since this would definitely be a “fair weather” vehicle there was no worry that these tires were “extreme performance summer” rated tires.

We installed the tires and had them “Road Force” balanced using the latest equipment from Hunter.  This ensured that the tires were not only balanced, but were a round assembly that would roll true.

After a test drive it was clear that the car needed some help beyond the tires in order to achieve a proper level of handling performance.  We dug into Flyin’ Miata’s catalog and chose items that would stiffen up the chassis as well as give us a bit more power.

They have what they call a Cannon rear subframe brace that provides stability for the rear suspension as well as a “butterfly brace” that provide fantastic rigidity to the under chassis.  We had installed this brace on the ’96 and found it to be a huge benefit.

The owner wanted to replace the factory Bilstein shocks with Koni adjustable shocks.  I must admit that I was more in favor to keeping the Bilsteins since I have always been impressed with their performance on other cars, but we discovered later that his decision was a fortuitous one. 

We wanted to get the ride height to look better than it did.  The rear appeared to be a little too high for the car when you viewed the fender gap.  So I went online and checked what was available from the folks at Swift Springs.  My experience with their product has been very favorable.  They have a spring technology that is currently the best around with a small diameter wire, they are lighter and use less coils, all of which contribute to less unsprung weight, without the coil sag we have seen in other springs.  They had a set that would work perfectly with this Miata.  The Swift fronts are rated at 202 pounds/inch and the rears at 157 pounds/inch.  They would drop the front 1.0 inches and the rear 1.2 inches.  Our experience with the Swift Sport springs was that they did not compromise the ride in any way or fashion which was particularly important for this owner.

Flyin’ Miata has a sway bar (a.k.a. roll bar) set that removes a certain amount of body roll without compromising the ride.  This was another excellent choice that would really improve the fun factor of this car.

The owner wanted a little more power out of exhaust system modifications without irritating his neighbors.  He picked out Racing Beat four-into-one headers and Racing Beat muffler.  He also chose a Randall cowl induction kit from Flyin’ Miata.

He also had some maintenance items he wanted attended to such as a fresh set of spark plugs, wires, and coil pack.  While the coil pack might seem like overkill, it had been a problem area mentioned in several forum entries so it could pre-empt some ignition troubles.  The brake and clutch fluid needed to be flushed and that meant it was a prudent time to replace the flexible brake hoses with braided stainless steel versions.  The brake pads and rotors were, of course, in fine shape.

Since seven thousand miles were on the odometer it was also a good time to change the oil and filter.  We use Mobil 1 5W-30 for this car.

In the interests of safety a Hard Dog padded roll bar was added to the list of parts.  In my opinion, this should be mandatory in any convertible.

With all this stuff on order the project was just started.  Now we had to plan out our process for making all those upgrades and changes.  I went over and over in my head just what each area would take in terms of tools and effort and what the best order might be to do all these changes in.  The weekend was approaching and parts were piling up.

Saturday morning I drove out to pick up the car, still thinking over just what would be done when.  A local shop, Performance Chassis, would provide lift time so I could get the most possible accomplished over the weekend. 

The Miata and I arrived and I brought it up on the lift so I could get a good look at things.  The shocks and springs were a good starting place and the rear was where I would begin.  That gave the exhaust system time to cool before I started on that.

First thing to be removed was the wheels in order to have complete access to the suspension parts.

To start on the rears the anti-roll bar needed to be disconnected as well as the upper control arm and lower shock bolt.  The trunk was cleared out of all the grey trim pieces and the gold colored plate covering the fuel lines was unbolted and removed as well.  That provided access to the two nuts that held the top of each shock assembly in place.  Once they were removed the car went back up in the air and the lower control arm was pried down so the shock assemblies could be removed. 

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When the assemblies were taken apart on the wall-mounted spring compressor there was a shocking surprise (no pun intended).  The bump stops on the rear shocks had become just oily pink powder.  Apparently the shaft seals on the rear shocks had dried out and pumped shock oil onto the bump stops which dissolved them.  A quick call was put into the local Mazda dealership’s parts department and new bump stops were ordered.  They would be in early in the week so it meant that the new shocks and springs would go in, but would have to be pulled out again to have those essential pieces installed.

Bump stops are critical because they keep the shocks from bottoming out and breaking the internal valving or bending the shock rod.  The owner was cautioned to be especially careful with railroad crossings and pot holes until the bump stops were installed on the rear shocks.  With the new springs a single hump would be cut from each bump stop as required by Swift, but to go without any would be a bad thing long term.

Each shock and spring assembly was put together using the factory rubber spring mounts, but the metal washers between the rubber insulators were drilled out for the larger Koni shock rods.

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The rear shocks and spring went in beautifully. 

Before tackling the front shocks the exhaust had cooled down enough for some preparation work to go on.  First the O2 sensor had to be loosened and removed from the old exhaust.  It was important to keep the twist in the wire so that when it was crew in to the new header it would finish up with the wire being straight so I wedged it in a convenient place that would hold the twist.  Then I removed the nuts from each of the exhaust flanges including the rear muffler.

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I find that to remove exhaust prongs from the black rubber hangers it is best to pry the rubber holes with a narrow screw driver and spray in some silicon lubricant.  This allows the rubber to slide off easily releasing the exhaust component.  The rear muffler came off easily and the new Racing Beat version took its place just as easily.  A new gasket was provided and everything bolted up just like it was a factory piece, only it looked and would sound far nicer.

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Now was a good time to add the Cannon rear subframe brace.  It meant removing four nuts, two of which were the lock-down nuts for the rear alignment eccentrics.  To make certain that I didn’t move things too far out of whack I marked the eccentric washers and the scale on the subframe before I removed the nuts. 

The brace slipped over the exhaust pipe easily and a cross piece was bolted on to complete the brace assembly.  Then the unit was slipped over the four bolts and the nuts were torqued back in place.  That would really stiffen things up in the rear.

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I lowered the car again so I could undo the nuts holding the top of the shock mounts and the strut tower brace that came with the car. 

With those out of the way I unbolted and removed the air filter housing from the fender so I would have access to the exhaust manifold.  Since this Miata had so few miles accumulated it was easy to unbolt the heat shields and loosen the EGR connection.  Then it was just about as easy to loosen and remove all the nuts holding the exhaust manifold in place.  There is certainly plenty of room to work on that engine.

The EGR fitting was completely loosened and gently pried out of the way while the manifold was pulled off the head.  The lower pipe just prior to the catalytic converter was also removed by undoing two bolts that held the transmission to the engine.  These two bolts also held a bracket connected to the exhaust.  The bracket would be discarded but the bolts would be re-installed to hold the transmission to the block.

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It was very easy to slip the new Racing Beat header into place.  There was plenty of room and it fit like a glove.  The EGR fitting also slipped on and was easy to tighten.  This was important because it is usually a place where it would be easy to cross-thread the fitting. 

The original exhaust gasket was re-used.  This it typical as it is a robust piece anyway.  Then the nuts were fit on each of the head studs lightly before the car went up in the air again so the exhaust flange could be bolted together at the cat. 

It was a little tricky to get the new gasket in place and lined up properly before tightening down the flange nuts.  I found that a flashlight, screw driver and patience was needed to ensure a proper seal.  With that accomplished I reinstalled the O2 sensor making certain that the wires were straight when it was tight.

Then back down went the car so the header nuts could be tightened to the specified torque.

We connected up the air filter box so we could test start the engine and make sure there were no exhaust leaks.  None were found and everything sounded as good as it looked.

It was time to get back to the front shocks.  The lower control arms would have to be unbolted at the alignment bolts so, like the rear, the eccentrics were marked to the subframe and then they were unbolted.  These are two bolts used to adjust the front camber and the caster.

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This time it was a matter of pulling down on the upper control arm so the shock assembly could be removed.

The spring compressor allowed the disassembly of the unit and this time the bump stops were intact.  The gold metal washers had to be drilled out large enough to fit the Koni’s larger shock rods, but everything went together well and it was barely challenging to get it put back into place.

The lower control arms were bolted up and the eccentric marks allowed us to get the settings very close to their original places.

In order to get the top shock nuts back on the car would be lowered once again, but since the strut bar was out of the way it was a good time to change out the ignition parts.  New wires were inserted in the new coil pack and then the old plug wires were removed from the spark plug wells.  The old spark plugs were wrenched out and proved to be in good shape, but with gaps that had been closed up quite a bit.  New plugs went in and the old coil pack was replaced with the new unit and wires.  Then the strut tower brace was put into place and the shock mount nuts were tightened down to specs.

Up to that point it had been a ten hour day and we took a break so that we would not be making any foolish mistakes.  There would be plenty of time available on Sunday.

The next day it was time to get the Hard Dog roll bar in place.  Since the butterfly brace would be installed as well, it was a good time to unbolt and remove the seats as well as clear away the items required for removal prior to the Hard Dog install.

There are excellent instructions available on their web site so I won’t go in to all the details here.  The biggest challenge is to take your time trimming the plastic trim pieces to fit around the bar.  It is a great safety item and the fit and quality cannot be beat.  It is made in North Carolina so the shipping time was a day.

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After the bar was the challenge of the butterfly brace.  This is made up of five pieces of specially fabricated stainless steel.  Their installation requires the carpet be pulled up because there are many holes to be drilled and bolts to be fastened through the floor.

It is mandatory to have some help with this one.  So I enlisted the aid of Rodney, perfectionist extraordinaire, to handle the duties on the ladder while I drilled and bolted from below.

First to be installed are the frame rail reinforcement pieces.  This brought some frame damage to our attention.  The reinforcement pieces would not fit over the rail because the rails had suffered damage from the misuse of floor jacks.  The factory rails had to be hammered back into shape before the new pieces could fit over them.  Measurements were taken to make certain that things were still square and then the rails were set in place and the first holes were drilled.  After the first set of bolts were nutted up the second brace pieces were bolted to the new rails.  They were kept loose so that the center section could be bolted in between.

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This requires a lot of tedious and careful work so I was fortunate to have Rodney’s help, but the results are always incredible.  This bracing provides much needed rigidity, especially with the damage that the factory rails had suffered.

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While there was still energy left I changed the oil and filter and then got the car off the rack.  I was anxious to see and feel the improvements as well as get it back to the owner so he could experience the transformation.

The car will be back for the installation of the rear bump stops as well as the FM anti-sway bar kit, braided stainless steel brake lines, cowl induction, and fresh brake fluid.  We also want to try for an alignment where we can put in more caster. 

So enjoy this phase of the transformation and look forward to next weekend’s completion.

Here are some photos to hold you.

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Ken Block – Gymkhana Training

August 8, 2009

Ken has made a well deserved name for himself in American rally competition.  He entered a gymkhana event in southern California and decided to convert a car he had to run in more events.  By the time the car was prepped the gymkhanas were cancelled.  So what to do?  He made this Gymkhana Practice video that Jeremy Clarkson of Top Gear thinks is one of the coolest motorsports videos he has seen.  Now you can see it too.


Corvette Z06 – You’re Busted.

August 6, 2009

The rumors had been accumulating.  Someone thought they saw a black Corvette on the beltline that had blue flashing lights and a car stopped.  Maybe it was true.

We have seen the local and state police use many types of vehicles in and around this part of North Carolina.  Usually it took the form of an unmarked Dodge Charger with heavily tinted windows and an officer with a LIDAR gun.   The state troopers have had special Mustangs and Z28 Camaros but this one goes above and beyond.

It is true, the Sheriffs Department got a hold of a seized 2007 Chevrolet Corvette Z06 and is using it for nabbing speeders and drug dealers.

Word is that they will be taking the deputies that will use the car to Virginia International Speedway to train them how to drive the Z06 at speed.  Many are waiting for the inevitable – when a deputy says, “hey y’all look at this!”